1Jan

Hyk2gjmac Hyk2gj For Mac

1 Jan 2000admin
Hyk2gjmac Hyk2gj For Mac 3,7/5 3889 votes

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Does anybody know how to import the auto complete emails from PC Outlook 2007 to Mac Outlook 2011? This is not the same as auto complete for words, but what happens when we begin to type in an email in Outlook and it shows us a list of emails to choose from. I imported contacts fine but don’t know how to do this. Sorry for the long winded question but want to avoid confusion.

  1. import 'Outlook.nk2
    The .nk2 file contains all the auto complete addresses for outlook in windows and is located in
    Windows XP:- C: drive:Documents and Settingsuser nameApplication DataMicrosoftOutlook.
    Windows Vista/7:- C: drive: usersuser nameAppDataRoamingMicrosoftOutlook
    You can copy the .nk2 file from the above locations.

    or use this soft the nk2 editor
    http://www.nirsoft.net/utils/outlook_nk2_autocomplete.html
    Install it> open the nk2.exe file> select all contacts> click on file> save selected items > in save as type choose CSV> ok
    Use this CSV format and then you can import it office 2011

    on MAC
    You will observe that the CSV file if imported directly, will not be displaying the desired information in Mac Outlook, under contacts. So you need to edit the CSV file, and delete all other fields except the 'Name' and 'Email Address' fields. Once the CSV file is edited, import it in Outlook for Mac using the Import option. You will now find all the contacts from the NK2 file under a new contact list in Mac Outlook.

    or you can instal thunderbird on both computers in windows you can import contacts as LDIF, then the file you add it on usb key and then transfer to MAC and ask thunderbird to import LDIF then will go to MAC office.

Hyk2gjmac Hyk2gj For Mac

This machine had dug up peat all of its working life and was in a fair condition and complete with all of its covers. It was a late production model with the later 580C Modifications.

Sevreral of the bolts around the slew ring had sheared off in the bedplate so there was no choice but to seperate the platform from the undercarriage. The boom and dipper arm were first removed and then the remaining bolts from the slew ring. A 30 ton Daewoo took very little effort to lift the 580C platform from the undercarriage.

Undercarriage

The tracks were then split. They are the 30 ins grouser pads which are 6 inswider than the standard pads and offer less ground working pressure from working on peat moors (some Hymacs were specially equipped with 48 ins wide pads for this type of work).

There was very little wear on the track pins and the bushes so they were re-fitted.

The undercarriage was completely stripped of all of its component parts including the bottom rollers. Undercarriage welding (later production machines) had the thicker wall cross tubes and the tub so there was no need for any welding. The undercarriage was shot blasted and painted.

The idler wheel bearings had not collapsed but were dry of any lubricant and could not be knocked out, so the assemblies were taken to Finning (CAT) to be pressed out. The idlers were then rebuilt using new bushes and new face to face seals. The shafts cleaned up fine. The track adjusters had both new seals and chrome bars fitted.

The bottom rollers were shot blasted and painted. The top rollers had flats worn onto them and were replaced.

The track drive gearbox components were all cleaned and checked and the brake fastener pinions replaced, along with bearigs and seals and gaskets. The brake shoes were relined and the brake cylinders resealed.

The final drive assemblies, which are piece part built into the frame on the Hymac 580C, were all checked for wear. It was the heavy duty final drive with a thicker drive shaft (later production). The drive sockets were blasted and painted. The shafts and bearings were cleaned along with the retianers and spacers. The face seals were renewed.

Transfer of movement from the gearbox to the final drive sprocket is via a heavy duty roller chain. They had stretched and were replaced. The track drive gear drive motors were were stripped. The motors were reconditioned and then run on a test rig to confirm both pressure and delivery.

The platform had the same treatment of blasting and painting, all the tanks being cleaned both before and after then sealed.

Hydraulics

Elm327 software. The hydraulic pumps on the Hymac 580C are gear type hamworthy 2100 series triple in line design directly driven from the engine flywheel through a flexible coupling. There were fitted to the test rig before being stripped to check the flow rates as the machine was very slow especially on tracking. The reading weren't too bad when tested from cold however the oil soon became hot, which is a good marker for worn pump components, and the test rig readings soon fell away drastically, especially on the two front pump sections.

A new pump would give a 10% fall off in flow at 2,000psi. The readings demonstrated that this was where the sluggish tracking was coming from. When i stripped down the pump and saw the model plate and serial number, this was the original pump some 30 years old, turning at 2,000rpm.

The pump was recoinditioned using all off the shelf parts. The reassembled pump was put back on test and under load the flow figures showed that the pump was now operating like new.

The valve blocks (Dowty Husco Type) were stripped and all pressure set while hot on the test rig.

Slewing Motor

It was a Staffa radial piston type slew motor and had very good inner components, slippers, pistons and crank lobe etc.

However, the crankshaft itself had a crack that ran from the bottom of the pinion keyway which had been due to the pinion working loose. A new crank was ordered and the motor was rebuilt using new bearings and seals.

Slew Rig

The slew rig was the Raballo type and some of these rigs have a double row of steel ball bearings but this was the taper roller type where each roller is fitted through a plugged hole in the bearing wall. This is a pre loaded bearing making the last rollers very difficult to get in to the track.

The slew ring is fitted to a seperate bedplate with the motor and pinion bolted in, the bedplate can then be adjusted to give the correct backlash in the teeth.

The slewrig assembly was then fitted back on to the undercarriage and the platform dropped back on and bolted down. At this stage all of the platform components were refitted including all of the control linkages which had been overhauled.

Engine

The Perkins 6,354 engine that was in the machine was a good runner with plenty of power but had an annoying knock (suspected little end bearing). I did have a Ford 2703E engine from a Hymac drilling rig and it was decided to fit this motor along with the Hymac / Ford skid frame. Hymac used both makes of engine in the production. Tje buld up engine powerpack and repaired canopy were refitted and all fuel pipes re-connected.

All of the hydraulic lines were re-connected, making sure that the lines to the front end were sealed off as it had not yet been refitted. The hydraulic tanks were filled with 90 gallons of fresh oil and the system bled of air. At this point there were no electrics back on the machine apart from the reconditioned started motor and alternator so a jump battery was fitted.

With full throttle and the excess fuel button engaged the engine burst in to life after a couple of turns. With the hydraulic gear pump circuits the full flow of the 3 pumps is immediately picked up and dispensed around the pipework, so with over 70 gallons per minute of fresh oil thrashing about its a frantic run round to check for any leaks in the system. With the machine now having hydraulics to the final drive, the tracks were able to be pulled on and adjusted to the correct tension.

Front End Equipment

All of the hydraulic cylinders had their seals replaced and the rod eye was replaced on the dipper ram. The welded bosses in the dipper arm were all worn and it was sent out to Strutt engineering which manufactured and welded new bosses in to place ensuring they were correctly aligned.

The front end equipment was then re-fitted with new pins and bushes and the pipework connected. The machine had already been painted the front end equipment had been painted off the Hymac.

The rotted cab base was plated, shot blasted and painted and the glazing rubber replaced. A new wiring harness and dash panel were made up by Howard Webster, a former Hymac electrician.

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